Li'l Jo Construction Log

The Maxitrak Li'l Jo kit was purchased from Barry Bridges via the Discover Live Steam for sale page. Barry had ordered the engine as a mogul wheel configuration and with a 2 axle tender. From the notes that Barry provided with the engine, there were a few issues with the parts that were supplied. Barry kept a wonderful notebook with the instructions and ideas that he had for finishing the engine. Barry had only gotten as far as assembling the running gear when he sold the kit to me. He had painted the frames flat black and the drivers were black spokes with white rims. Because of the move to Colorado, this project got put on the back burner until recently. I have started working on the engine and will be updating this page as I proceed. I must also thank Keith Manison for his extremely detailed description of building a Maxitrak Pearl. His website has gone away, but he allowed me to make a copy of it before it went down for the final count. I refer to it regularly when trying to understand the instructions provided by Maxitrak. There are a number of differences between the Pearl and the Li'l Jo, but there is enough in common to make it very helpful.



02/16/2008

I started with an assessment of what has been done and what needed to be done next. Barry had assembled the rolling gear and after some lubrication, it seems to be smooth enough. I have found a few steps that seem to have either not been done, or done out-of-order. The first issue is with the valve gear. The crank arms are suppose to be bracketed by cotter pins on the weight shaft to keep them in position. Also, the swing arms are suppose to be pinned to the crank arm cross shaft. Currently, if I rotate the running gear by hand, the cross shafts will eventually work there way so that they hit each other. Here is a close up of the swing arms and cross shaft.




Another issue is with the cylinders. The instructions call for the cylinders without the valve chests to be mounted on the frame and connected to the drive rods before the valve chest is mounted. As received from Barry, the valve chests were already mounted. Luckily, Barry has not used LocktiteŽ on anything yet, so it should be fairly easy to remove the valve chests so that the assembly matches the instructions.

Last issue (may not be and issue) is with the mounting of the foot plates for the cab. The instructions call for the footplates to not be mounted until assembling stage 4 step 2. Barry has already mounted them. The boiler is made of copper and has a lug on each side of the firebox that rests on the frame.  This lug is then held in place by a small angle plate that holds the lug to the frame. Barry has already mounted the foot plates. So, I may need to unmount them to put the boiler on the frame. The instructions are not clear, the diagram in figure 15 looks like it should be mounted upside down compared to how Keith mounted them on his Pearl. The footplates on the Li'l Jo extend above the frame, so maybe it's okay to have the footplates mounted at this stage.





02/17/2008

I decided to make my first real assembly step the mounting of the saddle. The saddle is a welded sheet metal affair that has been pre-drilled with the mounting holes that match holes in the frame. It is held in-place by 5 nut/bolt pairs on each side. (Barry had already painted it flat black.) The frame has a notch for the steam pipes to the valves. The saddle has to be modified so that there is space for the steam pipe to pass through the saddle and frame notch. I did this by mounting the saddle to the frame and marking the location of the frame notch on the saddle. I then removed the saddle and cut a wood block to fit between the two sides so that it would not distort while I was drilling the "notch hole". I then used a 1/2" bit to drill a hole in saddle. Then I used a Dremel tool with a fiberglass cutting blade to make hole into a slot.



After this, I test fit the boiler to see how things lined up and to check the main steam pipe from the throttle. I will need to make a similar notch for the steam pipe. This will wait until I am ready to fit the boiler.



As you can see from the second picture, the main steam pipe is going to need some re-bending to make it fit properly. I guess that is to be expected as this kit was shipped from the UK to Arizona, then Michigan, then Ohio, and finally Colorado. I have tried to anneal the pipes using a simple propane torch, but I can't seem to get them hot enough to glow red. I also tried some MAPP gas for a hotter flame, but that did not work either. I will have to revive my Oxy/Acetylene torch to get the heat I need.

I also had to drill out the hole for the blast pipe in the bottom of the smokebox to 1/2" size. As shipped, the hole was closer to 3/8". I did not take a picture of this, but the blast pipe is now a tight fit into the smokebox.


02/24/2008

The first task for today was to add cotter pins to the swing arms. For the moment, I have decided not to pin the crank arms to the weight shaft ... they don't seem to need it. I discovered that I need to get a better center punch. The drill bit wandered, but the holes are done and the pins are in as you can see in this photo.



I had previously removed both cylinder blocks from the frame. I removed the valve chest from the right cylinder and proceeded as stated in the instructions. I remounted the cylinder (after removing the front cover) and check for the length of the piston rod. The instructions call for there to be a 1/8" gap between the connecting rod and the piston rod when the piston is 1/8 of an inch from the front of the cylinder.



I cut the extra off (in place) with a Dremel motor tool and cut off disk. The next step was to mount the crosshead guide and connect the connecting rod to it. The steps here consisted of filing the sides of the end of the connecting rod a bit so that it would fit into the crosshead. Then, I attached the crosshead to the end of the connecting rod using the supplied bearing rod and nut. Next, I used a piece of threaded rod to make a stud for bolting the crosshead guide to the cylinder. The crosshead guide was not drilled for the bolt that would attach it to the motion bracket, so I marked it and drilled the needed hole on the drill press. (The instructions are vague on the bolt to use here ... I guessed.) I could not find the listed motion bracket spacers in the kit, so I put a pair of washers in for now. Once all this was done, the whole mechanism seems to move easily when turning the drivers.



I remounted the valve & valve chests and checked the valve drive rod. The instructions call for the rod to be bent in an S shape to line up with the valve rod. I ran out of time, so that will have to be left until next time. Here is the current view of the right side ... starting to take shape. I am hopeful that 2 more sessions will get me to the point that I can run the chassis on air.



02/27/2008


I finished up the left-hand side to match what I did on the right. This time, I removed the motion bracket and swung the connecting rod up so that I could put the crosshead on the end of the rod more easily. That save me endless time fiddling with the bearing/fastener that pins the rod to the crosshead. When I did the right hand side, it was very difficult getting that pin into the crosshead and rod from from between the rod and the drivers. The finished job looks like this:



The next step is to bend the valve rods, time the valves and button up the cylinders for a test on air ... so close ...


03/02/2008

As mentioned from the last time, I needed to bend the valve rods so that they lined up with the valve crosshead. The instructions simply indicate that an S bend is necessary. You can see in this picture why the bend is necessary:



I marked both valve rods 1 inch from each end with a magic marker. I took them to my drill press vice and chucked them to the lines that I had drawn and gently, but firmly bent them into the required shape. Here is one mounted up after being bent to shape: (The bearing slipped out for the picture ...)



The next step was to set the valves. The instructions (to me) are a bit cryptic. I made my best attempt at it, but to me, it looks like there is way too much motion in the valves. The instructions indicate that there will be more motion in reverse than forward, but it still seems too much. Anyway, after setting up the valves as best I could, I put the front cylinder covers and valve covers on. I also put on the brass cylinder head and valve covers because their attachment screws penetrate the covers that they attach to. You have to put them on the seal everything up. I decided to try running the chassis on air. I made up a fitting that allowed me to attach the compressor to the steam line.

Drum roll please ... it works!!! The motion is not smooth and there seems to be a lot of blow-by as the exhaust line has a constant stream of air even when the mechanism is stopped. Currently, it seems to run no slower than 20psi, but I imagine this will improve as it gets worked in. It will self start if the pressure is high enough.

Now for the bad news, I had a lockup when running in reverse. Basically, the eccentric strap and swing arm end up as an inverted V instead of a regular V shape.  I think the issue is that reach rod pushes the swing arms too far forward and that allows the eccentric strap to flop upward occasionally. The instructions call for moving the reverser stand backward or forward to adjust this. I think I will have to do that. Here are some pictures of the chassis in motion.



03/03/2008

After asking on the Home Shop Machinist live steam forum (http://www.chaski.org/homemachinist/), I re-lubricated the valves and cylinders with 32 wt motion oil that I have had for ages and ran the chassis on air again. It seems to do better, but it is still rather stiff. After running for ~10 minutes, I disconnected the air and found that it was much easier to turn the drivers by hand.

I decided to look at mounting the axle pump. It mounts to a slightly angled tab on a frame stretcher. As near as I can tell, this is not going to work. The pictures show that to screw the pump into the frame stretcher, the pump hits the axle. So, I could drop the axle to get the pump installed, but if I screw it into the frame stretcher, the "T" end of the pump will be right where the axle goes.

Hitting the axle ..



If screwed in as far as it goes until it hits the axle, the pump arm is just about out of the throat when the eccentric strap is furthest away. The o-ring just starting to show ...



If I did screw it in, it would be in the way of the front axle ...